Date Range
Date Range
Date Range
PN4206 Sumo Challenge Groups 2015. PN4206 Sumo Challenge Groups 2014. PN4206 Sumo Challenge Groups -Spring Semester, 2014. SEOIGHE CAOMHAN MR, MC GRATH KEVIN MR, MC GIRR MICHAEL MR. CAMPION EOIN MR, COUGHLAN GEAROID MR, DORGAN KIERAN MR. BOLGER SHANE MR, CROGHAN MARK MR, TOBIN ALAN MR. WHELAN MICHAEL MR, GUERIN ANTHONY MR, KEATING MICHAEL MR.
Thanks for dropping by danger1989! Take a look around and grab the RSS feed. Mdash; Leave a comment. We used circuit wizard to make the program for the robot. Mdash; Leave a comment. Mdash; Leave a comment. The bucket is a bit far away from the servo that is one of our mistakes we made and if we were doing it again i would shorten the arms for the loader. Mdash; Leave a comment.
Here is a quick video showing the motion of our lifters via the servo motor and the fishing wire. Finished covering and bot nearly done. Coming towards the end we realised our PCB was left very exposed, initially we decided that we would leave the robot without a covering. However, then we decided it was in danger of damage so we made a covering from cardboard.
On April 24, 2012. The inside of the robot is relatively spacious to allow room for the circuit board and other components as can be ssen from the images below. On April 24, 2012. On April 24, 2012.
Connecting the flipper to the armature. Again we had trouble doing this we had planned on using a round bar to attach it but the bar kept snapping every time it was bent. Wiring the components and assembling the robot. The brackets were made from aluminium and pop riveted into places.
To activate the flipper, a switch was needed. To increase the chance of the opposition hitting the switch, we made a switch which covered the full width of the front flipper. to do this, springs were needed at each end of this surface so the switch could be activated easily. We could alter the sensitiveness of the switch once we had the wiring completed.